/W3C//DTD HTML 4.01 Transitional//EN"> The Rev 5 Page

DOM MB Rev 5 Home Page

If changes consist of corrections to the schematic, and no changes to the copper, then the version will change to 5.n.
If changes involve modifications to the circuit topology, then the version will change to 6.0.

Versions:

What's new in  Rev 5.0: Significant changes from Rev 4 to Rev 5.0

What's new in Rev 5.1: well... not much. Solder terminals and the test connector have been moved.

Study of behavioral details

Off-Board (Flasher board) Pulse Monitoring Input Study

Trigger Comparator Input Signal Study

fADC shaping amplifer Study

DOM MB i-v curve Study

Common Clock Study i.e. supplying coherent clock signals to DOR card and DOM MB

DOM Gain presentation

Photo Gallery

Rev 5.0 image files 

Pictures of an integrated DOM, including sphere, PMT, PMT base, flasher board, HV power supply, and the DOM Main Board .

The Rev 5.0 photo gallery. Images of the DOM MB by itself, or with delay card mounted.
Rev 5.0 PowerPoint figures

Rev 5.1 Main Board Image

Main Board TIFF image Annotated filtered DOM MB image
8 megapixel, TIFF, JPG 30% PDF 640K, 20% PDF 636K, 30% JPG 960K, 20% JPG 876K Line art PDF; 660K, Image file JPG; 1700K
Main Board TIFF image Annotated filtered DOM MB image (rotated)
8 megapixel, TIFF, JPG 30% PDF 676K, 20% PDF 676K, 30% JPG 3600K, 20% JPG 704K Line art PDF; 660K, Image file JPG; 592K

Rev 5.1 PowerPoint figures

IR Images

ICE3_IR_40-1800x1200.bmp
ICE3_IR_40min2.jpg
ICE3_IR_40-overlay.pdf

Lighter is warmer. The orange block on the right hand side is a reference temperature source.
Reflective objects may appear to be colder than they actually are because they reflect the surrounding temperature.
The image was taken roughly 40 minutes after the power was turned on.

Production

V5.0 production:

The first small production run consisted of contract fabrication with debugging done by LBNL. HASS testing, was done by an outside contractor; burn-in and integration testing were done at LBNL. Orders were based on an expected yield of 80% without rework. Rework was required to raise the yield above ~60%, and ultimately resulted in a yield of ~95%.

A few late corrections, and changes were deemed sufficient, and safe enough to warrent a minor redesign of the DOM MB. (See the revision list for details) The result was V5.1

V5.1 production:

The second year production involved splitting the work between two vendors as part of the ramping up of output. The first half of the production duplicated the first year paradigm. The second half of production used a single vendor contract manufacturer which built, debug, ran HASS test, and burn in boards with LBNL supplementing debugging.

The third year production was done by single vendor contract manufacture, chosen by competitive bid. Unlike previous years, the contractor committed procuring all components (except a few that LBNL made lifetime buys on), and to only deliver good boards. The manufacturer achieved well over 95% yield, mostly due to the skills of their own technical staff debugging problem boards, with a little bit of supplemental help by LBNL engineers.

Pre-delivery diagnosis pages...

Collected analysis of V5.0 and V5.1 DOM MBs
[documentation has lagged a little behind repairs; there are more trouble reports than entries in the HTML list]
[some boards are not completely diagnosed, but instead, assigned into software test subsystems]

Post-Deployment diagnostics...

Disgnosis of DOM failures in the ice at the south pole are somewhat speculative, since it is not possible to probe the board in situ as much as 2500 meters below the south pole. All diagnostics must be based on data collected by the DOM itself, and transmitted to the surface.

From Mark Krasberg's powerpoint, presented at the collaboration meeting, April 12, 2006